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Energy Audit at Dairy
plant at Rajkot,Gujarat. |
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A comprehensive
energy conservation study of the Dairy plant at Rajkot,Gujarat.
was carried out by PCRA.This Dairy is engaged in the manufacture
of various qualities of milk & also other milk products
like buttermilk, flavored milk & ghee in their plant.
The total milk received per day is around 1.0
Lakh litres . Annual Production of the plant Liquid milk –
28023 MT,Ghee – 651.7 MT,Flavored milk – 1133.1
MT.There is one. boiler-, furnace oil fired 1.5 TPH, for generating
steam for use in the plant.
Daily furnace oil consumption is 429.27 Kl .The unit takes
its electricity supply from the GEB .The contract demand is
300KVA. Electricity is consumed in a variety of equipment
in the refrigeration plant compressors & auxiliary equipment
like cooling & chilled water pumps, air compressors, water
& milk pumps & lighting.Annual electricity consumption
is18.19 LakhKWH
A comprehensive energy conservation study
of the plant was carried out by PCRA, The identified total
annual energy saving potential is around Rs. 25.857 Lakhs
on a recurring basis. The energy audit has identified several
areas for energy conservation in thermal & electrical
energy. The steps identified for energy conservation are given
below:
- The excess air levels in the boilers is slightly on
the higher side. It is recommended that the unit
procure a combustion analyzer & reduce the excess
air levels such that the oxygen % in the flue
gases is 3.0%. This will result in improvement in boiler
efficiency.
- Furnace is stored in 2 nos. main storage tanks of capacity
30000 lts. At present there are no drain points installed
on the tank. It is recommended that drain points be installed
& storage tanks be drained at least once a fortnight.
This will ensure that all the water is removed from furnace
oil & prevent sludge formation.
- It is observed that the municipal water is directly
used as boiler feed water. The municipal water
has a hardness of 75-80 ppm. It is recommended that the
raw water be softened to have hardness
below 5 ppm before using it as boiler feed water. This
will prevent scaling of boiler tubes as well
as all the steam heat exchangers in the plant.
- Steam line insulation was in good shape in the plant
in. However, some the valves & flanges on
the PRV stations are not insulated in the plant. It is
recommended that the valves & flanges be
insulated with box type insulation to reduce radiation
losses. Also, some lengths of steam lines are bare near
the can washer as well as in both the old & new CIP
sections. It is recommended that the bare steam lines
be insulated as soon as possible.
- Presently, steam is directly sent to the process section.
It is observed that steam is directly injected into one
section in the can washer as well as in pasteurizer hot
water tanks & crate washer. It is recommended that
a pressure reducing station be installed to reduce the
steam pressure to 2.5 kg/cm2g before sending it to these
sections.
- It is observed that the steam valve to the CIP hot
water tank is continuously on. It is recommended that
an auto temperature controller be installed such that
the steam supply will be closed when the 8 desired hot
water temperature is reached.
- The actual regeneration efficiency of the milk pasteurizer
is very low at 71.8 %. It is recommended that the pasteurizer
be descaled. This will reduce the steam as well as chilled
water load in the pasteurizer drastically.
- Condensate is recovered from the main line steam traps.
It is recommended that hot water
overflow from the pasteurizer hot water tank as well as
the CIP hot water trap be recovered &
supplied to the boiler feed water tank.
- The power factor of the plant is not satisfactory.
The average power factor for the dairy is 0.987. It is
recommended that the power factor be improved to unity
consistently. This will result in savings in electrical
bills.
- The contract demand for the dairy is 300 KVA. It is
observed that the actual maximum demand
has consistently crossed 340-350 KVA. It is recommended
that the contract demand be increased
to 375 KVA. This will reduce the penalty payable on excess
maximum demand & lead to a
reduction in the electricity bills.
- Thus the efficiency of the hydroflow pump is too low.
Thus it is recommended that the pump be
replaced by a higher efficiency pump having efficiency
of 70%. This will reduce power
consumption for water pumping.
- It is observed that water pumps & milk pumps are
frequently burnt out due to milk/water leakage
through the seals leading to moisture in rotor /stator.
It is to be noted that the efficiency of an
induction motor reduces with every rewinding. It is thus
recommended that motors which have
been rewound frequently be replaced with high efficiency
new motors. This will lead to an overall
reduction in power consumption in the plant. It is also
recommended that the pump seals be replaced on a monthly
basis as a preventive measure to prevent leakage. This
should help in reducing the number of motor burnouts in
the plant.
- After milk pasteurization, the milk temperature is
still on the higher side at 16 deg c. It is chilled to
1.5 – 2.0 deg c. It is recommended that the milk
be chilled upto 4 deg c. This will lower the
refrigeration load on the chilled water.
- As has been mentioned in section 5.7.4, the milk pasteurizer
has an actual regeneration efficiency 9 of 71.8% as against
a theoretical efficiency of 90%. It is recommended that
the PHE be descaled so as to achieve regeneration efficiency
of 90% once again. This will reduce chilled water refrigeration
load significantly.
- It is observed that chilled water is used during CIP
of tanks & silos using iodoform. It is
recommended that chilled water be replaced by raw water
. This will reduce chilled refrigeration
load.
- It is recommended that the unit install an instant
chiller PHE for reducing the load on the IBT. This will
facilitate a 70% reduction in the refrigeration load on
the IBT thus allowing reduced ice
thickness on the ammonia coils. Due to reduced ice thickness,
the average suction pressure can be raised to 40 psi from
the present average of 30 psi. This can be taken up when
the unit decides for modernization of refrigeration section.
- The unit receives 75 kl per day of corporation water
. Presently around 15 kl of corporation water
is used in boiler & the rest is mixed with borewell
water. This is due to lack of water storing
capacity. It is recommended that the unit store the clean
corporation water in a separate tank & use it for
cooling water make up as well as for process water use.
- It is also observed that the natural draft cooling
tower is quite old. It is recommended that the unit replace
it with a PHE condenser & a forced draft cooling tower.
This will result in at least 10%
reduction in power consumption in the refrigeration compressors.
- It is observed that the high pressure ammonia discharged
from the ref compressors is at a high
temperature of 100 -110 deg c. It is recommended that
the unit install a de-superheater (PHE heat exchanger)
to recover waste heat from the high pressure ammonia discharged
from the
refrigeration compressors. The waste heat can be utilized
to generate hot water which can be used in CIP hot water
tank as well as can washer, crate washer & for floor
cleaning points.
- A walk through audit of the plant during the shut down
period revealed that there were compressed air leakages
in a number of locations near the pouch packing machines
especially in the air regulators. It is recommended that
the leakages be identified & eliminated on a weekly
basis. This will reduce power consumption in the air compressors.
- Compressed air is generated at a pressure of 6.5-8.0
kg/cm2g in the diary. The pneumatic valves
require a minimum pressure of 6 kg/cm2g. Thus the pressure
setting of the air compressor is is on the higher side.
It is recommended that the cut-off pressure be reduced
to 7.5 kg/cm2g initially & 10 eventually to 7.0 kg/cm2g.
This will reduce the average compressed air generation
pressure to 6.75 kg/cm2g as against the present 7.5 kg/cm2g
leading to power savings.
- Present lighting single phase voltage is 240 to 245
volts. Nowadays lighting transformers are
available, which reduce the voltage to around 210 volts.
The reduction in voltage also reduces power consumption
with little reduction in lumens emitted by the light source.
The savings due to
installation of lighting transformer is 15-20% of the
power consumption.
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| For further information, please write to:
Director (I/C),
PCRA,
Sanrakshan Bhawan, 10,
Bhikaji Cama Place,|
New Delhi-110066
Telephone: +91-11-26198856
Fax. +91-11-26109668
Web site: www.pcra.org |
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