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Energy Audit at Dairy
plant at Palanpur, Gujarat. |
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A comprehensive
energy conservation study of the Dairy plant at Palanpur,
Gujarat was carried out by PCRA.This Dairy is engaged in the
manufacture of various qualities of milk & also other
milk products
like butter, ghee, ice cream as well as milk powder in their
plant. There are 2 plants – plant I –
which is old & handles can reception & plant- II ,
which is modern & handles chilled milk reception The
milk processing capacity is 3.3 & 5.3 lakh litres per
day for Plant & Plant II respectively.Annual furnace oil
consumption is 4555 MT for Plant-I and 3866 MT for plant-
II.The unit takes its electricity supply from the GEB .The
contract demand is 1400KVA & 2000 KVA for Plant I &
Plant II respectively.
A comprehensive energy conservation study
of the plant was carried out by PCRA, The identified total
annual energy saving potential is around 169.05 lacs on a
recurring basis. The energy audit has identified several areas
for energy conservation in thermal & electrical energy.
The steps identified for energy conservation are given below:
- The excess air level in all the boilers is satisfactory.
However, some fine tuning can be done such
that the oxygen % in the flue gases is 3.0%. This will
result in improvement in boiler efficiency.
- Furnace in the main storage tank is heated by steam
coils. This results in churning of the furnace oil &
does not allow the moisture present in the furnace oil
to settle down. It is recommended that steam heating in
the main storage tank be stopped. It is also recommended
that the furnace oil storage & service tanks should
be drained at least once a week.
- It is observed that the steam coil in one of the furnace
oil storage tanks is leaking. It is recommended that this
be rectified as soon as possible.
- Furnace oil main storage tanks should be cleaned at
least once a year to remove the sludge
accumulated at the bottom of the tanks.
- During the audit study, it was observed that the autoblowdown
valve was continuously blowing for
at least 5 – 10 minutes & the TDS value of the
boiler water was not coming below 3700 ppm. It is
recommended that the autoblowdown TDS should be regularly
cross-checked with samples tested in the laboratory. Moreover,
it is recommended that a timer can be installed on the
blowdown valve such that it is closed after a certain
time period.
- It is recommended that heat from the blowdown from
Plant I boiler be recovered by installing a
blowdown heat recovery system.
- Steam line insulation was in good shape in the plant.
All the valves & flanges are not insulated in
the plant. Also some bare steam lines were observed. By
insulating with 2" thick mineral wool with aluminium
cladding, 90% of the heat loss can be minimised.
- A steam trap survey was conducted in the plant. Steam
traps identified as leaking /blocked should be rectified
immediately.
- Condensate should also be recovered from the 20 TPD
plant & ghee plant. The unit is already
thinking in this direction.
- Condensate from the 30 TPD plant is at a very high
pressure. The present condensate recovery
system installed does not recover the flash steam. It
is recommended that flash steam recovery
system be installed for recovering heat from the flash
steam.
- It is recommended that the air heaters in 30 TPD plant
in Plant I & 60 TPD plant in Plant II be
tuned to reduce the excess air levels
- It is recommended that the supply air quantity for
the 60 TPD spray dryer be reduced such that it is at design
flow rate of 97000 kgs/hr. Further the supply air temperature
should be raised to 185 deg C. It is to be noted that
with addition of additives to the furnace oil , the flue
gas temperature will not rise above 230 deg c. Thus, the
supply air temperature can be raised to 185 deg c. This
will result in savings of at least 10% of furnace oil
in the 60 TPD air heaters. We suggest that trials be conducted
on the spray dryer. Only if the trial is successful, these
savings will be realized.
- Design air flow rate is not available for the 30 TPD
plant. However, the present air flow of 70128
kgs/hr seems to be on the higher side. The unit is advised
to reduce the air flow by 5% initially. This will result
in an increase in supply air temperature & exhaust
temperature. The milk flow will have to be increased to
reduce the exhaust temperature to the original level of
90 deg c. It is estimated that savings of at least 5%
can be achieved due to reduction in supply air flow to
the air heater. This requires a detailed analysis from
the unit. We suggest that trials be conducted on the spray
dryer. Only if the trial is successful, these savings
will be realized.
- Due to reduction in supply air flow by 10% in the 60
TPD plant, the power consumption in the
Supply air fan can be brought down by 27%. Also power
consumption in the exhaust fan will also
come down due to reduction in air quantity. Thus it is
recommended that the VFD be installed on the supply air
fan to reduce its air flow & generate power savings.
This is connected to the trial of reducing air flow in
the 60 TPD plant. Only if the trial is successful, these
savings will be realized.
- The power factor of the plant is not satisfactory.
The average power factor for Plant I & Plant II is
0.986 & 0.977 respectively. It is recommended that
the power factor be improved to 0.999. This will result
in savings in electrical bills due to increase in rebate
amount.
- The rated head of soft water & DM water pumps is
quite high at 60 meters. It is recommended that the soft
water & DM water pumps in the WTP section be replaced
by new pumps with the same capacity & lower rated
head & the throttling of the discharge valve reduced.
- It is recommended that one large pump of 200 m3/hr
with a rated head of 35 meters head be installed. The
chilled water flow normally required is around 200 m3/hr.
Thus instead of operating 4 pumps in parallel only one
large pump can be operated with its discharge valve fully
open.
- The rated head of the condenser & the cooling tower
pumps are high at 20 meters. Normally 2 sets of condenser
pumps & 2 sets of CT pumps are in operation in the
plant. Presently these pumps are operating in throttled
conditioned. It is recommended that the impellers of all
these pumps be trimmed by 10%. This will reduce the head
delivered by these pumps by 19% & also reduce the
power consumption by at least 20%.
- A few underloaded motors have been identified during
the audit study. If the load on these motors is constant,
the motors can be replaced by lower HP motors from the
store/inventory.Alternatively, the motors should be connected
permanently in star connection.
- The booster compressor in Plant I has an evaporator
temperature is – 53 deg c corresponding to a suction
pressure of 0.33 bar. The ice cream cold store temperature
required is – 30 – 35 deg c. It is recommended
that the evaporator temperature be raised to – 45
deg c. This will reduce electricity consumption in the
booster compressors by at least 15 %.
- The ice cream deep freeze & the ice cream hardening
room were converted from conventional cold stores. However,
the insulation was not upgraded during the conversion.
Thus , it is observed that the temperatures of the adjacent
room to the ice cream deep freeze is as low as 11 deg
c. It is recommended that the insulation be upgraded .
This will reduce the cooling load on the refrigeration
system drastically.
- Presently the – 10 deg c system in Plant II is
operated at a suction pressure of 3.14 bar
corresponding to a saturated suction temperature of -8.3
deg c. It is recommended that the – 10 deg c system
be operated at -5 deg c. This will result in power savings.
- It is observed that milk is underchilled in the plant.
During the audit study, we observed pasteurized milk temperatures
ranging from as low as 3 deg c. This is a direct loss
in terms of steam as well as of refrigeration capacity.
It is recommended that the plant personnel be more vigilant
& throttle the chilled water valves incase the milk
flow in the pasteurizers is not as per the rated capacity
of the unit.
- It is observed that the insulation of chilled water
supply & return lines to Plant I is quite poor as
seen from the moisture condensation on the surface of
the lines. It is recommended that the
insulation be upgraded at the earliest.
- It is recommended that mechanical pouch packaging machines
be installed for replacing the 2nos
pneumatic machines presently in operation in the pouch
packing section.
- It is recommended that the compressed air requirement
for powder plant pneumatic conveying
system should be met by the central plant screw compressors.
However, presently excess
capacity is not available with the central compressors.
After the pouch packing machines have been replaced by
mechanical ones, excess capacity will be available .
- There are a large number of pneumatic control valves
in Plant II process section. During the audit study a
leakage round was taken with a leakage identification
instrument. The leakages were pointed out to the plant
personnel. It is recommended that these leakages be eliminated
immediately. It is also recommended that the unit procure
the instrument & conduct regular leakage surveys in
the plant.
- Present lighting single phase voltage is 250 to 260
volts. Nowadays lighting transformers are
available, which reduce the voltage to around 220 volts.
The reduction in voltage also reduces power consumption
with little reduction in lumens emitted by the light source.
The savings due to
installation of lighting transformer is 30% of the power
consumption.
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| For further information, please write to:
Director (I/C),
PCRA,
Sanrakshan Bhawan, 10,
Bhikaji Cama Place,|
New Delhi-110066
Telephone: +91-11-26198856
Fax. +91-11-26109668
Web site: www.pcra.org |
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