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Energy Audit at Dairy
plant at Anand, Gujarat. |
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A comprehensive
energy conservation study of the Dairy plant at Anand, Gujarat.
was carried out by PCRA.This Dairy is engaged in the manufacture
of various qualities of milk & also other milk products
like cheese, ghee, and ice cream in their plant.The total
milk processed yearly is 17000 Kl . Annual Production of the
plant Pouch – 17067 kl, Buttermilk – 1471.8 kl
,Ghee - 378.3 MT,Cheese – 322.3 MT,Ice cream –
536.02 kl,Paneer - 22.17 MT.There are 2 nos. boilers- 3 TPH
each, for generating steam for use in the plant. The boilers
use furnace oil as fuel. Annual fuel consumption is 237.7
KL. The unit takes its electricity supply from the GEB .The
contract demand is 450KVA. Electricity is consumed in a variety
of equipment in the refrigeration plant compressors &
auxiliary equipment like cooling & chilled water pumps,
air compressors, water & milk pumps & lighting. Annual
electricity consumption is 22.82 LakhKWH.
A comprehensive energy conservation study
of the plant was carried out by PCRA, The identified total
annual energy saving potential is around Rs. 10.5 Lakhs on
a recurring basis. The energy audit has identified several
areas for energy conservation in thermal & electrical
energy. The steps identified for energy conservation are given
below:
- The excess air level in all the boilers is satisfactory.
However, some fine tuning can be done such
that the oxygen % in the flue gases is 3.0%. This will
result in improvement in boiler efficiency.
- It is also recommended that the furnace oil storage
& service tanks should be drained at least once a
week. Furnace oil main storage tanks should be cleaned
at least once a year to remove the sludge accumulated
at the bottom of the tanks.
- Furnace oil preheating is presently done by electric
heaters. The 2 nos. steam heaters should be used &
electric preheating of furnace oil should be stopped.
Furnace oil is preheated upto 110 – 115 deg c which
is correct practice.
- Presently, the furnace oil pressure to the burner is
set at 16 kg/cm2g. It is recommended that the
furnace oil pressure to be raised from present level of
16 kg/cm2 to 20 kg/cm2 for proper atomization.
- It is recommended that heat from the blowdown from
Vidya I boiler be recovered by installing a
blowdown heat recovery system.
- Boiler blowdown is manual for the boiler. Boiler water
should be checked periodically for TDS level.
Blowdown level should be optimized based on permissible
TDS level of 3500 ppm.
- Steam line insulation was in good shape in the plant
in. However, some the valves & flanges on the PRV
stations are not insulated in the plant. It is recommended
that the bare valves & flanges be insulated.
- Condensate is not recovered from all the powder plant.
Presently, an Ogden pump has been installed for the CIP
PHE. However, it is not functional. It is recommended
that the condensate from the CIP PHE be recovered. Also
condensate from the cheese vat can be recovered as the
quantity is significant.
- The hot ammonia gas is discharged from the KC -4 compressor
at a temperature of 110 – 120 deg c. It is recommended
that a desuperheater be installed to preheat boiler feed
water.
- It is recommended that the contract demand be reduced
from 450 KVA to 400 KVA. This will reduce the MD charges
payable.
- There are 2 nos. IBTs in the plant. One IBT is sufficient
for meeting the chilled water load of the
entire plant. The ice thickness maintained in the IBT
is 5”. It is recommended that the overall ice
thickness maintained in the IBT be reduced to 4”.
- Presently, the compressor cylinders are unloaded manually
based on the suction pressure. It is
recommended that the compressor cylinders be unloaded
automatically & the suction pressure be
maintained between 30 – 40 psi. This is possible
if the IBT thickness required is 4” as against 5”
maintained earlier. Similarly, the booster compressor
should be maintained 5 – 10 psi.
- It is suspected that the air supplied by the cooling
tower fan is less than required. It is recommended that
the cooling tower manufacturer be contacted for increasing
the air flow through the cooling towers. Alternatively,
the plastic fills of the cooling tower are choked &
need to be replaced.
- It is recommended that the condensers be chemically
descaled. This will allow operation of only one condenser
& also reduce the discharge pressure of the compressor
resulting in power savings.
- The rated head of condenser & cooling tower water
pumps is quite high at 25 meters. It is
recommended that the impellers of these pumps be trimmed
by 10%.
- It is observed that the cream storage tank chilled
water collecting pot is undersized & overflows
from periodically. It is recommended that the sump capacity
to be increased to avoid overflow.
- It is recommended that the AHU fans be shut off when
the required temperature is achieved & the ammonia
supply is cut off from the AHU coil. This can be implemented
for milk cold store/butter cold store.
- It is recommended that mechanical pouch packaging machines
be installed for replacing the 5nos
pneumatic machines presently in operation in the pouch
packing section.
- Present lighting single phase voltage is 250 to 260
volts. Nowadays lighting transformers are
available, which reduce the voltage to around 220 volts.
The reduction in voltage also reduces power consumption
with little reduction in lumens emitted by the light source.
The savings due to
installation of lighting transformer is 30% of the power
consumption.
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| For further information, please write to:
Director (I/C),
PCRA,
Sanrakshan Bhawan, 10,
Bhikaji Cama Place,|
New Delhi-110066
Telephone: +91-11-26198856
Fax. +91-11-26109668
Web site: www.pcra.org |
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