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Energy Audit at Dairy
plant at Navsari, Gujarat. |
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A comprehensive
energy conservation study of the Dairy plant at Navsari, Gujarat.
was carried out by PCRA.This Dairy is engaged in the manufacture
of various qualities of milk & also other milk products
like buttermilk & ghee in their plant. The total milk
received per day is around 2.35 Lakh litres .
Annual Production of the plant Liquid milk – 88014.5
tonnes,Buttermilk - 1250 tonnes. Ghee - 149.8 tonnes.There
are 2 nos. boilers-, both coal fired 2 TPH each, for generating
steam for use in the plant. One boiler is in operation &
the other is stand by. Annual consumption Coal consumption
is 1618tonnes. The unit takes its electricity supply from
the GEB .The contract demand is 850KVA. Electricity is consumed
in a variety of equipment in the refrigeration plant compressors
& auxiliary equipment like cooling & chilled water
pumps, air compressors, water & milk pumps & lighting.
Annual electricity consumption is 38.62 LakhKWH
A comprehensive energy conservation study
of the plant was carried out by PCRA, The identified total
annual energy saving potential is around Rs. 25.738 Lakhs
on a recurring basis. The energy audit has identified several
areas for energy conservation in thermal & electrical
energy. The steps identified for energy conservation are given
below:
- It is observed that the coal size fed to the boiler
is not uniform & is around 4-5”. It is recommended
that the coal size be uniformly maintained at 2.5”.
This will help in complete combustion of coal & reduce
unburnt % in the ash content. It is recommended that the
unit procure a coal crusher such that the uniform coal
size is obtained.
- It is recommended that the height of the coal bed be
maintained at 8”. This is the optimum bed height
for achieving good combustion with minimum excess air
levels.
- The flue gas temperature for one of the boilers is
in the range of 250 -260 deg c. It is recommended that
the unit should install a waste heat recovery economizer
to generate hot water
for boiler feed. This will result in fuel savings
- Steam line insulation was in good shape in the plant
in. However, some the valves & flanges on the PRV
stations are not insulated in the plant. It is recommended
that the valves & flanges be insulated with box type
insulation to reduce radiation losses.
- It is observed that the CIP PHE is presently bypassed
& steam is being used in the CIP PHE at a pressure
of 6 kg/cm2g. It is recommended that the CIP PHE be made
operational & the steam utilization pressure be reduced
to 3-3.5 kg/cm2g.
- It is observed that the can washer PRV is not in operation
& steam is utilized at a pressure of 6 kg/cm2g. It
is recommended that the PRV be made operational &
the steam pressure reduced to 3 kg/cm2g. This will reduce
the steam consumption in the can washers.
- It is observed that the can washer PRV station safety
valve is leaking. It is recommended that the safety valve
be rectified as soon as possible to reduce steam consumption.
- It is observed that the CIP PHE float traps are connected
to the condensate recovery system via
same header. This results is back pressure on the steam
traps & the operator thus has to keep the bypass open.
It is recommended that the steam traps be connected to
the condensate recovery system through separate lines.
This will increase condensate recovery from the CIP PHE.
- The unit has also installed a desuperheater on the
old refrigeration compressor. The unit is sending solar
water into the desuperheater with the result that waste
heat recovery is not optimum. It is recommended that the
unit send soft water to the desuperheater. This will optimize
the waste heat recovery.
- Presently, CIP hot water is drained . The quantity
of CIP hot water drained is approximately 100000 litres/day.
The temperature of the hot water drained is around 60
deg c. It is recommended that the unit install a waste
heat recovery PHE to recover waste heat from the hot water
presently drained. This will enable the unit to generate
hot water at 50 deg c which can be used in the CIP tanks.
Since it is contaminated water, investment for additional
PHE of proper capacity V/s its feasibility is to be worked
out by the unit.
- The power factor of the plant is not maintained consistently.
It is observed that it fluctuates from month to month.
The average power factor for the dairy is 0.992. It is
recommended that the power factor be improved to unit
consistently. This will result in savings in electrical
bills due to increase in rebate amount.
- It is observed that the water/milk is leaking from
the pump seals of the milk/water pumps. This sometimes
finds it way into the motor resulting in frequent motor
burnouts. This results in frequent rewinding of the pump
motors , resulting in a drop in their efficiency &
consequent overloading. It is recommended that the pump
seals be inspected & changed on a monthly basis to
reduce water/milk eakages & reduce motor burnouts.
Moreover, it is recommended that motors which have been
ewound more than 5 times can be considered for replacement
with new high efficiency motors. This will result in savings
of electricity.
- As the suction pressure of the new refrigeration plant
is maintained at a higher pressure of 42-45 psi as compared
to the :old refrigeration plant , it is recommended that
both the prechillers & the compressors installed in
the new plant be operated in series. This will reduce
the overall power consumption in the refrigeration plant.
The unit is conducting a trial as discharge gas line of
old system & PHE system is made common between Vertical
condenser outlet & Receiver inlet with diff. Dia.
pipe lines.
- After operating the two new PHEs in series , the refrigeration
storage capacity can be reduced. Thus the ice thickness
range can be reduced from the original 1.5 “–
2” to 1.0 “– 1.5 “. This will
allow an increase in the suction pressure to 35-40 psi
thus leading to at least 5% power savings.
- In the old refrigeration plant cooling tower area,
it is observed that the suction valves of the cooling
tower pumps are throttled. It is recommended that the
cooling tower pump impellers be trimmed by 15%. This will
reduce the flow by 15% but will reduce the discharge pressure
by 27%
to 18 meters which is more than sufficient for the cooling
tower. The power consumption in the
pumps will reduce by more than 30%
- It is estimated that the air compressor operates on
load for 60% of the time & on unload for 40% of the
time. The unload power consumption is wasteful & can
be eliminated by installing a variable frequency drive
on the compressor. It is recommended that the unit establish
the average running hours of the compressor on load &
unload. Based on these figures, the unit can evaluate
the economic viability of the VFD drive.
- Present lighting single phase voltage is 250 to 260
volts. Nowadays lighting transformers are available, which
reduce the voltage to around 220 volts. The reduction
in voltage also reduces
power consumption with little reduction in lumens emitted
by the light source. The savings due to
installation of lighting transformer is 30% of the power
consumption.
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| For further information, please write to:
Director (I/C),
PCRA,
Sanrakshan Bhawan, 10,
Bhikaji Cama Place,|
New Delhi-110066
Telephone: +91-11-26198856
Fax. +91-11-26109668
Web site: www.pcra.org |
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